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This article by Stefan Vorkoetter originally appeared in the
February 2004 issue of
QuietFlyer
magazine and is reproduced here with permission.
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What About the Wires?
In recent months, I've had the opportunity to build and/or review a
number of parkflyer models, along with the electronic equipment
designed specifically for such models. Although the models have all
flown reasonably well, one thing that has bothered me is the use of
relatively thin battery and motor power wires and connectors in
parkflyer speed controls and battery packs.
My e-flight instincts were telling me that a significant amount of
power is being wasted in these thin wires, and that it ought to be
possible to do better.
Larger models, typically operating at about 25 Amps use 14 gauge (2
mm²) or 12 gauge (3.3 mm²) wire to minimize losses at these
current levels. Speed 400 models, which usually draw about 10 Amps,
generally use 16 gauge (1.3 mm²) wire.
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The GWS ICS-300 speed control, as it comes from the factory, together with the motor wiring Y-harness provided with the GWS BN-2 Islander park flyer. All wiring is 22 gauge.
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This Great Planes ElectriFly C-10 speed control also uses 22 gauge wire.
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An Experiment
The GWS ICS300 speed control that came with my GWS BN-2 Islander
review model comes equipped with 22 gauge (0.3 mm²) battery and
motor leads, terminated with tiny two-pin connectors. The speed
control is rated for 8 Amps continuous current, yet the wires are
only slightly thicker than those in a servo lead (which typically has
to carry no more than 0.5 Amps).
Also part of the BN-2 review model was a Y-harness to split the
output from the speed control to drive two motors. This Y-harness,
and the motor leads themselves, are also 22 gauge wire.
Finally, there is the battery pack. Although I did not use a GWS
battery pack, I assembled my own, using the same power lead that GWS
and Great Planes use on their parkflyer battery packs.
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My home-made 7x750 NiMH battery used a stock park-flyer power lead, again with 22 gauge wire.
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The total length of wire (including both the positive and negative
leads) from the battery to the split in the Y harness was 28 inches
(71 cm). In addition to this, there was a tiny connector between the
speed control and the battery, and another between the speed control
and the Y-harness.
I decided to try to replace as much of the wire as possible with
high-flex silicone insulated 16-gauge wire as would typically be used
in an 8 to 12 Amp model. Before doing so however, I measured and
recorded the propeller RPM at full throttle with a fully charged
battery.
What to Replace?
Ideally, I would have replaced all the wiring, but the motors and
their leads are inaccessible in the finished BN-2 model, so I decided
to leave them with 22 gauge leads. This isn't quite as bad as it
sounds, as each motor lead only needs to carry the current for a
single motor. For the same reason, I elected not to replace the
Y-harness-to-motor connectors and the wiring after the split in the
Y-harness.
I did replace the battery input and motor output leads of the speed
control, and the power leads of the battery itself. I also replaced
the battery connectors with 4-pin Dean's plugs, which have more
contact area per pin (and more of them) than the standard parkflyer
plugs.
First I modified the Y-harness by removing the heat-shrink from the
joints, and cutting off the input lead and connector (that would have
attached to the speed control output). I replaced the input leads
with short lengths of 16 gauge wire.
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A close-up of the GWS speed control with the heat-shrink covering removed. There's lots of room to attach heavier wires.
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Another close-up of the GWS control. The 22 gauge motor and battery wiring has been replaced with 16 gauge.
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Replacing the speed control wiring required a partial disassembly of
the speed control. First I carefully slit the heat-shrink covering
with a knife, and peeled off the GWS label which covered the wire
attachment points. The original motor output wires were soldered into
holes in the circuit board, but this was not possible with the larger
replacement wires (the Y-harness' input wires). Instead, I just
soldered the positive (red) wire to the positive bus bar, and the
negative (black) wire directly to the pad connected to the center pin
of the MOSFET.
The original speed control power input wires were already soldered to
the positive and negative bus bar. I unsoldered them, and soldered
the new wires in their place. The other ends were each soldered to
two pins of a 4-pin Dean's plug. After completion, I slipped a new
piece of heat-shrink tubing over the speed control, and used a heat
gun to shrink it. I left off the GWS label, because I was afraid the
gold foil might short-circuit the new input wires, which protruded
past the label.
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The completed speed control. All power wiring between the battery connector and the split point in the Y-harness has been replaced with 16 gauge. The Y-harness is soldered directly to the speed control, and the battery connector has been replaced with a 4-pin Dean's plug.
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The battery pack also received new 16 gauge leads, terminated by a 4-pin Dean's connector.
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The procedure for changing the battery wires was just as simple. I
removed the existing heat-shrink, unsoldered the 22 gauge wires,
soldered on the new 16 gauge wires with 4-pin Dean's connector, and
re-covered the pack with a fresh piece of heat-shrink tubing.
The net change was to replace 28 inches of 22 gauge wire with 18
inches of 16 gauge wire, replace one connector with a better one, and
eliminate one connector entirely.
The Results
The results speak for themselves. Originally, with the battery fresh
off the charger, initial RPM was 9,360 rpm, dropping to 9,240 after a
few seconds, and remaining there for a few seconds. With the
replacement wiring, RPM started out at 10,320 rpm, dropping to 9,900,
where it remained for a while. This represents a 7% rpm increase,
which doesn't sound like much at first. However, when propellers are
involved, output power is proportional to the RPM cubed, and this
increase translates into a 23% power increase. That's like adding an
extra cell to the 7-cell battery! Table 1 summarizes the results.
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Wire Gage
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Length
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Connectors
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RPM
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Power (est)
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Before
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22 gauge
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28 in.
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2 - tiny
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9240
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31.4 W
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After
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16 gauge
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18 in.
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1 - Dean's
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9900
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38.6 W
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Table 1. Results of Wire and
Connector Replacement
The Theory
This wouldn't be Demystifying Electrics if I didn't explain why the
changes made such a big difference.
The key word here is "resistance". Long thin wires have
more resistance than short fat ones. The resistance of a wire is
proportional to both its length, and its cross-sectional area (which
is proportional to the square of its diameter).
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An extreme close-up of two wire cross-sections. The larger 16 gauge wire is on the left, 22 gauge on the right. The 16 gauge wire is twice the diameter and four times the cross-sectional area.
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The original 28 inches of 22 gauge wire had a resistance of about
0.038 Ohms. The 18 inches of 16 gauge wire that replaced it is only
0.006 Ohms, giving approximately a 6-fold reduction.
The remaining reduction came from the replacement of the tiny 2-pin
battery connector with a 4-pin Dean's connector, and the elimination
of the speed-control-to-Y-harness connector.
Using a high-current power supply, an ammeter, and a voltmeter, I
measured the voltage drop across both types of connectors and
computed their resistance. The 2-pin parkflyer connector has a
resistance of 0.007 Ohms per pin. With two connectors in the circuit,
there are four pins, for a total resistance of 0.028 Ohms. The Dean's
connector on the other hand has a resistance of 0.00085 Ohms per
pin-pair. With such connector, there are two pin-pairs in the
circuit, for a total of resistance is 0.0017 Ohms.
Adding together the resistance eliminated by the better wires, and
better and fewer connectors, the resistance went from 0.066 Ohms down
to 0.0077 Ohms, a savings of 0.058 Ohms. At 8 Amps, the original
wiring produced a 0.53V drop. The new wiring loses only 0.062V. That
means there would be a 0.47V increase in voltage reaching the motor
(which represents about an 8% voltage increase). In reality, the
voltage increase will be slightly less, because the increased voltage
will cause the motor to draw more current, which will increase the
losses in the wiring somewhat.
Was It Worth It?
Yes indeed! Climb performance has increased noticeably, especially
from a hand launch, and the model can maintain level flight at half
throttle.
Contrary to my intuition, the change of the wire alone did not have
as much effect on the performance as did the replacement and/or
elimination of the connectors, but the calculations show that it did
make a significant contribution to the improvement nonetheless.
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My simple yet effective RPM testing set-up. A Globee tachometer sits behind the propeller, and a flashlight on the far workbench provides a bright flicker-free light source so the tach will read accurately (house lights, even incandescent ones, cause the tach to misread).
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Lower wiring and connector resistance does more than just increase
the maximum power available; it can also increase flying time.
Although the full throttle current has gone up, flying time is not
reduced as long as the throttle is used properly. The decreased
resistance means greater system efficiency, which means that one can
throttle back further and have the same propeller output power as
before, but at a lower current. The result is increased flying time.
There was a very slight increase in weight (from 14.8 oz to 15.0 oz)
caused by the heavier wire and connectors, but compared to the power
gained, this is insignificant.
In Conclusion
Electric flight has become mainstream, and there are now many mass
market products out there to choose from. Unfortunately, these have
not been optimized as much as the earlier products made by the
smaller, specialized, electric flight manufacturers. The result is
equipment that, although it works, doesn't work as well as it might
if the manufacturer had expended just a little more effort. Suitably
sized wire and decent connectors can make a huge difference in
performance, at very little increase in cost.
I recommend that if you want to get the most from an off-the-shelf
parkflyer power system, that you look carefully at where the losses
are. Even if you don't want to go through the trouble of
disassembling the speed control to install thicker wires, at least
cut the wires to the minimum length needed, and use better
connectors.
Finally, for very low powered models operating in the 1 to 3 Amp
range, the extra effort may not be worth it. At lower currents, the
voltage losses are less, and hence there is not as much to gain. But
if your model's performance is marginal, it might still be
worthwhile.
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Last updated Tuesday May 29, 2007.
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E-mail Stefan
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Disclaimer:
Although every effort has been made to ensure accuracy and
reliability, the information on this web page is presented without
warranty of any kind, and Stefan Vorkoetter assumes no liability for direct or
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The text and images of this article are Copyright © 2004 by
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