![]() |
|||||||
|
Electronics Reviews |
Electronic Projects |
Electric R/C Planes |
General Aviation |
Hammond Organs |
Calculator Collection |
Slide Rule Collection |
|
However, one type of component that is prone to wearing out, regardless of how little or how much a piece of equipment was used, is the electrolytic capacitor. A capacitor consists of two electrodes separated by an insulating material (dielectric). Capacitors store electric charges and block the flow of direct current through them while allowing alternating current to pass. An electrolytic capacitor is one where the insulating layer is porous and impregnated with an electrolyte solution (somewhat like a battery). The characteristics of this electrolyte change over time, potentially affecting the capacitance. There is also a risk of short-circuits forming, which can result in the capacitor leaking or exploding. The corrosive electrolyte can damage wiring or the chassis, but more importantly, the sudden failure of the capacitor can cause damage to much more expensive components such as the vacuum tubes that are relying on it to do its job. Capacitors in the M-100 Series AO-29 Amplifier
There are a total of ten electrolytic capacitors in the AO-29 amplifier. Two of them are on top of the chassis in the large black "can" to the left of the intermediate transformer (when viewed from the back of the organ), four more are in the silver can to the right of transformer, three are on the wiring boards inside the chassis, and one wired directly to a tube socket. It is possible to purchase replacement can capacitors from sources such as Tonewheel General Hospital but these are relatively expensive. I opted to replace the cans with separate electrolytic capacitors of the appropriate values instead. The following table summarizes all the capacitors to be replaced:
I ordered the replacement capacitors from
Digi-Key
(along with new capacitors to replace the aging wax-paper ones in the
vibrato line box and
Although it is theoretically possible to replace the capacitors with the
amplifier still in the organ, it would have been extremely awkward, so the
first step was to remove it from the organ. This required unsoldering a row of
connections along the back of the amplifier, including the AC power connections
enclosed by a metal cover and some shieled audio signal connections under
another cover. To ensure I'd be able to reconnect everything properly
afterward, I took several close-up photos of all the connections before
starting.
Next I undid the four bolts that hold the amplifier chassis to the floor of the
organ and carefully lifted the amplifier out. I debated whether I should remove
the tubes before or after extricating the amplifier, and decided to wait until
the amp was on the workbench. I was afraid that a hard-to-remove tube might let
go suddenly and that I would smash it against something in the organ.
After carrying the amplifier to my workbench, I carefully removed each tube,
placing them in consecutive compartments of an egg carton. I inspected each
tube as I removed it to make sure I could still read its markings in case I
managed to mix them up in the carton. Once all the tubes were out, I set them
aside, out of harm's way.
Before beginning, make sure that any high voltages stored
in the capacitors have been discharged. Using a clip lead, connect one end
of a 1kΩ resistor to the chassis. Then using another clip lead, touch
the other end to each capacitor positive terminal for a few seconds.
The first step in replacing the cans was once again to photograph everything in
great detail. In addition to the photos, I drew a diagram indicating all the
connections and where they lead to. Finally, I marked each wire to identify the
terminal it was connected to. There are a lot of wires connected to the
capacitor terminals and many of them are the same colour, so I did everything
possible to avoid a later mix-up.
The following steps describe the work done to replace the black can (containing
two 50µF 450V capacitors, C62 and C62A).
I unsoldered the wires using a 45W soldering iron (not a soldering gun) and a
plunger-type solder pump. As I heated up each solder lug, I used the pump to
suck away most of the solder. I used desoldering braid to wick up most of the
remaining solder. With the solder gone, it was possible to unwrap the wire from
each lug and then heat it up once more to pull the wires out.
Once all the wires were off, I straightened out the twist-tabs holding the can
to the chassis and cleanly removed it. After removing the black can, there was
still the phenolic socket to remove. I did this by drilling out the rivets with
a 1/8" drill bit from the top side of the chassis.
To mount the individual replacement capacitors, I cut a piece of phenolic
perfboard 1.7" x 1.7". I drilled out three of the holes to 1/8"
diameter. Two of these corresponded with the existing rivet holes in the
chassis and the third was approximately in the centre of the perfboard.
Using 1/8" steel pop rivets, I riveted the board to the chassis and then
riveted a 4-position terminal strip to the underside of the perfboard. I
connected the two centre lugs together to act as negative terminal for both
capacitors. The two outer lugs were then for the positive terminals of each
capacitor. The capacitors were installed from the top side of the board, paying
careful attention to polarity and keeping the leads away from the chassis
edges, and their leads were passed through the holes in the appropriate lugs
underneath.
With the capacitors in place, all the wires were routed to their appropriate
lugs. After carefully checking the wiring against the original photos,
drawings, and the markings on the wires themselves, everything was resoldered.
The end result was quite neat (by 1960s point-to-point wiring standards).
The silver can differs from the black one in two ways: it contains four
capacitors instead of only two, and the negative terminal solder lugs are
fastened directly to the chassis instead of to an insulated socket. Since there
are four capacitors, I needed at least five solder lugs (at least one negative
and four positive terminals). Instead of a single 5-position terminal strip, I
used two 3-position strips with the mounting lug at one end of each. I fastened
one strip with each rivet holding the perfboard in place, which served to
connect the end lug to the chassis.
I cut a short length of 14 gauge solid copper wire and passed it through these
two end lugs, effectively forming one long negative buss passing diagonally
under the perfboard. Three of the four capacitors were then installed on top of
the perfboard with their negative leads connected to the copper wire and their
positive leads connected to individual lugs. No matter how I arranged things, I
was unable to fit all four capacitors above the chassis, so I installed one of
the 22µF capacitors (C66) underneath, connecting it directly to the
terminal strip lugs.
With the capacitors in place, I reattached the wires to the appropriate solder
lugs and then soldered everything.
The two 25µF 25V electrolytic capacitors, C30 and C64, are near the two
ends of the wiring board. Before removing the old ones, I marked the bottom of
the board with the polarity so I'd be sure to install the replacements the
right way around.
Removing the old capacitors was easy, just requiring a few seconds of the
soldering iron on the underside of each turret to melt all the solder within,
at which point the capacitor's lead could be pulled out. Installing the new
capacitors was the same process in reverse: melt the solder in the turrets
and push the leads in.
For some reason, I forgot to replace C67 and C70, which I did not realize until
I began to write this article long after reinstalling the amplifier in the
organ. Since these capacitors are not riveted in, thus just requiring
unsoldering and resoldering, I can probably replace them without removing the
amplifier. Fortunately, neither of these capacitors are as critical as the
power supply capacitors, and a failure would not likely damage any other
components. Both are used as filters in the bass pedal circuit.
While the amplifier was readily accessible, I decided it would be a good idea
to do some general maintenance:
The chassis was covered with what looked like dust but which was almost
impossible to wipe off. I suspect it was dust, held in place by a thin layer
of Hammond tonewheel oil that had accumulated over the decades. I removed
it using rubbing alchol, a rag, and a toothbrush.
Before embarking on this exercise, I was experiencing a problem with
crackling noises emanating from the speaker when the organ was played at
high volume. Consulting with the folks on
The Organ Forum
suggested that it might have been a tube moving in a dirty tube socket,
causing an intermittent connection, so I thoroughly cleaned all the sockets
using DeOxit D-5 spray.
I cleaned up all the external connection terminals using the solder pump
and desoldering braid to remove all the excess solder and rosin.
I had briefly looked into the amplifier when I first purchased the organ in
2008 and found one capacitor (C70) that had become disconnected from a tube
socket terminal (which is how I know that a failure of C70 won't cause any
damage). With the amplifier on the bench, I gave it a more thorough
inspection with a magnifying glass to check for other broken connections.
With all the capacitors replaced (except C67 and C70), I gave everything one
more check, comparing my rewiring against the original photos and drawings, and
also the schematics from the service manual for good measure. Everything looked
good, so I carried the amplifier back upstairs to reinstall it into the organ.
One last check and then I started the organ. After letting it warm up for 20
seconds or so, I tentatively pressed a key and was rewared with a note from the
speakers. A thorough check showed that everything was (still) working, except
the expression pedal. I quickly realized I forgot to reattach the pedal arm to
the side of the dog house.
With the expression pedal reconnected, I sat down to play something. Part way
through the piece, I heard what sounded like a capacitor going up in smoke (a
sort of whooshing sound). Strangely, there was no smoke and no smell, and
everything still worked. I looked behind the organ and everything looked fine.
I continued playing and the whooshing came and went. Usually, changing
anything (like turning the internal rotary
speaker on or off) would make the sound disappear for a while, but then it
would return.
Did it sound any different when I was done? No, but I didn't expect it to.
All of the old capacitors still measured very close to their stated values, so
they were still working as designed. Unlike
If you found this article useful, you may also be interested in my other
Hammond organ technical articles:
Disclaimer:
Although every effort has been made to ensure accuracy and
reliability, the information on this web page is presented without
warranty of any kind, and Stefan Vorkoetter assumes no liability for direct or
consequential damages caused by its use.
It is up to you, the reader, to determine the suitability of, and
assume responsibility for, the use of this information.
Copyright:
All materials on this web site, including the text, images, and HTML
mark-up, are Copyright © 2010 by Stefan Vorkoetter unless
otherwise noted. All rights reserved. Unauthorized duplication
prohibited. You may link to this site or pages within it, but
you may not link directly to images on this site, and you may
not copy any material from this site to another web site or
other publication without express written permission. You may make
copies for your own personal use.
|
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
SubscribeShare |
|
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||