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Hammond Organ Tonewheel Generator Capacitor Replacement and Calibration

The Hammond M-series organ service manual describes the operation of Hammond's tonewheel generator this way:

  
Click to enlarge.
Electrical impulses of various frequencies are produced in the "tone generator", which contains a number of "tone wheels" driven at predetermined speeds by a motor and gear arrangement.  Each tone wheel is a steel disc similar to a gear, with high and low spots, or teeth, on its edge (see figure 12).  As the wheel rotates, these teeth pass near a permanent magnet, and the resulting variations in the magnetic field induce a voltage in a coil wound on the magnet.  This small voltage, when suitably filtered, produces one note of the musical scale, its pitch or frequency depending on the number of teeth passing the magnet each second.

The phrase, "when suitably filtered", is key here. Unlike those organs which produce complex tones and then use filtering to achieve the sounds of traditional instruments (subtractive synthesis), the Hammond organ produces nearly pure sine wave tones and then combines these to create instrument sounds (additive synthesis). The relative proportions in which these are combined are controlled by the organist using the Hammond organ's harmonic drawbars.

Tone Filtering

  
Click to enlarge.
For this scheme to work, those pure tones must be as close as possible to pure sine waves. This was achieved by manufacturing the tonewheels with appropriately shaped teeth and then using electronic filtering to remove any harmonics generated by inaccuracies. Of the 91 tonewheels in a Hammond console organ, the filters for tones #49 to #91 consist of a capacitor and an inductor (in the form of a transformer). The schematic excerpt to the left shows one such filter.

The operation of this filter depends on a number of parameters: the value of the capacitor, the inductance of the transformer and the tonewheel pickup coil, and the impedance of the transformer and coil. Together, these components form a passive bandpass filter. Only two different capacitor values were used in the tonewheel generator: 0.255µF for tones #49 to #54 and 0.105µF for #55 to #91. Tuning each filter to the desired frequency was accomplished using transformers of different inductance values. Because both capacitors and inductors have very loose tolerances, the Hammond factory hand-matched each pair to achieve the desired result.

   Three tone generator filters from my 1962 Hammond M-111 with wax-paper capacitors. Click image for details.
Three tone generator filters from my 1962 Hammond M-111 with wax-paper capacitors. Click image for details.
Why Replace the Capacitors?

Hammond organs made before the mid 1960s used wax-paper capacitors in their tone filters. Over time, these capacitors have absorbed moisture, which will have increased their capacitance. For example, it is not uncommon for a 0.105µF capacitor to increase to 0.300µF or more over several decades. This increase will lower the resonant frequency of the filter so that it no longer matches the frequency being produced by the tonewheel. The result is a severe attenuation of the desired signal, resulting in a dull or muffled sound. It is similar to the effect you'd get by turning down the treble and turning up the bass on your home stereo's amplifier.

Why Recalibrate?

After each tonewheel generator was assembled, a technician would calibrate it. The strength of the signal produced by each tonewheel depends on the distance between the tip of the magnet and the teeth of the wheel, as well as the amount of attenuation in the filter. Without calibration, the tone signals produced by one wheel might be significantly stronger or weaker than those produced by the next. Calibration involves adjusting the position of each magnetic rod to achieve a desired output level for that tone. To further complicate matters, all the tones were not adjusted to the same level. Instead, they were adjusted to match a calibration curve to take into account such factors as the frequency response of the amplifier and tapering of the resistance wires leading from the tonewheel generator to the manuals.

Theoretically, this calibration need never be redone unless one of the magnet set-screws has come loose and the magnetic rod has moved. However, when the capacitors are replaced, their values will not be exactly the same as the originals were when they were new, due to component tolerances. Therefore, the amount of attenuation provided by the filter will also be different. The result can be noticeably different volume from one tone to the next, and a recalibration will be necessary to make the organ match the original calibration curve.

Capacitor Replacement Procedure

I'd previously replaced the wax-paper capacitors in the vibrato line box of my 1962 Hammond M-111 organ to great effect. The old capacitors from the line box had measured an average of 69% higher than their stated values. I suspected that the tone generator filter capacitors would have deteriorated to the same extent, with the resultant loss in tone quality, so I decided to replace them and then recalibrate the tone generator if necessary. The procedure outlined here applies to the M-100 series of spinet organs, but the principles and techniques are similar for all Hammond tonewheel models, including the venerable B3.

Obtaining New Capacitors

There are six 0.255µF and thirty-seven 0.105µF capacitors in the tonewheel generator of a Hammond organ. Unfortunately, neither of these values are available today, the closest being 0.27µF and 0.1µF respectively. The original capacitors were rated at 200V, so the replacements should be rated at least that high (although I'm not sure why the originals are 200V rated, since they are being used at the millivolt level).

I ordered my capacitors from Digi-Key. I ordered Digi-Key part numbers P3493-ND and P3488-ND, but these have since been discontinued by Panasonic. Suitable replacements are PF2274-ND (0.27µF) and PF2104-ND (0.1µF). Whatever you order, be sure not to purchase inexpensive ceramic disk capacitors as these may adversely affect the sound (see The Sound of Capacitors - Capacitor Linearity).

There are also vendors selling packages of capacitors, specifically for Hammond tonewheel generators, that have been hand-selected for uniform capacitance as well as ESR (equivalent series resistance). I personally feel that this is unnecessary since the original capacitors will not have been nearly as closely matched, so a recalibration will be needed no matter how perfect the new capacitors are. On the other hand, these kits take the guesswork out of ordering the parts. One such kit is this one offered by GOFF Professional.

   The tone generator exposed, ready for capacitor replacement.
The tone generator exposed, ready for capacitor replacement.
Setting Up

In the M-100 spinet organs, the generator is readily accessible by removing the generator cover. The cover is held by four screws at the front and seven at the back. The four at the front need only be loosened since they are in keyhole slots but the seven at the back must be removed. Although it's not strictly necessary, both lighting and access to the generator are improved by removing the top of the organ (by undoing four screws).

To provide more working space, it's also a good idea to unbolt the vibrato line box and lift it up out of the way. I did this and used masking tape to hold it up.

One needs very little equipment for the capacitor replacement: a soldering iron, needle nose pliers, small wire cutters, and a flat bladed screwdriver are the basics. Regarding the soldering iron, do not under any circumstances use a soldering gun. These generate strong magnetic fields which will damage the magnetic rods in the tonewheel pickups.

A shelf clamped to the organ provides extra work space. The oscilloscope is for measuring tone generator output.   
A shelf clamped to the organ provides extra work space. The oscilloscope is for measuring tone generator output.
In the photo at left, you'll see I clamped a small plywood shelf to the tonewheel generator shelf to give myself a work surface. This beats repeatedly bending over to the floor to pick up tools. A low chair or stool is worthwhile too if you don't want to have aching knees by the end of the day.

Also in the photo is my oscilloscope. This is not needed for capacitor replacement, but I used it to measure the output of each tone generator before (for interest's sake) and after replacing each capacitor (to determine if recalibration would be necessary). If you don't have an oscilloscope, a peak-to-peak millivolt meter can be used instead. An inexpensive digital multimeter will not work, because it reads RMS voltage, and usually only accurately at low frequencies (50 to 60Hz).

Getting to Work

With everything set up, I was ready to start working. I decided to do the entire job with the organ running since I wanted to measure each tonewheel's output. Having the organ on also let me test each wheel by playing a key on the keyboard. Assuming there is no defective wiring in the organ, this is a fairly safe procedure since the generator is producing signals of at most 30mV or so. Likewise, almost nothing you can do to the generator circuitry with a soldering iron and hand tools can damage the rest of the organ. A Hammond organ is not a modern, highly-sensitive piece of equipment! On the other hand, turning it on and off 43 times would probably have been harder on it.

   Tone generator output displayed on the oscilloscope. This one is about 21.5mV peak-to-peak.
Tone generator output displayed on the oscilloscope. This one is about 21.5mV peak-to-peak.
Before removing each old wax-paper capacitor, I used the oscilloscope to measure the peak-to-peak voltage at the filter transformer's output terminal. This is the terminal with a black wire leading away towards the front of the organ. I attached the oscilloscope's ground clip to the brass tab adjacent to the filter and clipped the probe to the short bare section of the black wire. I recorded the results in my notebook.

The actual process of replacing the capacitors is fairly straightforward but somewhat tedious. For the 0.255µF capacitors, which are mounted along the rear edge of the generator assembly and connected to their transformers with short wires, I first cut the wires off near the capacitor body. I could then unscrew the capacitor mounting clamp and remove the capacitor from the generator. Using the soldering iron, I heated up the transformer terminal that each wire was attached to and, once the solder was molten, carefully pulled the wire out. After that, I heated the terminals again and used a solder pump to remove as much solder as possible in preparation for installing the new capacitor.

Removing excess solder to allow insertion of the new capacitor leads. The terminal below the solder pump has already been cleaned. Notice the fine transformer wires!   
Removing excess solder to allow insertion of the new capacitor leads. The terminal below the solder pump has already been cleaned. Notice the fine transformer wires!
The process for the 0.105µF capacitors was slightly different. For those, I first cut the capacitor lead that was closest to the centre line of the generator, about half way between the capacitor body and the transformer terminal. I then heated up the opposite terminal and carefully pulled the capacitor out. Next I heated up the terminal still containing the cut off lead and pull that out with needle nose pliers. Once again, I reheated both terminals and sucked most of the solder out.

It is important to pay attention to the transformer wires. They are very fine, delicate, and hard to see. It would be easy to accidentally snag one with a tool or the tip of the soldering iron and break it. Reattaching it might pose some difficulty because there is little slack in these wires.

I chose to install each new capacitor immediately after removing the old one so that I could test it right away, but an alternative is to first remove all the old ones and then install the new ones.

Both the 0.1µF and the 0.27µF replacement capacitors were installed right on the filter transformers, since they were physically small enough to fit. I first bent the leads of each capacitor 90° outward, approximately in-line with the capacitor's bottom edge. I then bent one lead about 120° half way along its length and cut it about 1/4" past the bend, forming a small hook.

Preparing a new 0.1µF capacitor for installation.
Preparing a new 0.1µF capacitor for installation.
Squeezing the hook to form a secure mechanical connection.
Squeezing the hook to form a secure mechanical connection.

To install the new capacitor, I inserted the straight lead through the transformer terminal to which the tonewheel pickup coil is attached (the one with a coloured wire connected to it). Then I passed the hooked lead through the other terminal (the one with a single fine transformer wire connected to it). Using needle nosed pliers, I squeezed the hook shut, forming a firm mechanical connection. The straight lead at the other end was then bent upward and over the terminal and the excess cut off.

Bending and clipping the opposite lead before soldering.
Bending and clipping the opposite lead before soldering.
Soldering the connection to make it permanent.
Soldering the connection to make it permanent.

These steps were repeated for each of the 43 capacitors in the tonewheel generator. After each capacitor was replaced, I consulted the manual wiring chart from the service manual to find a drawbar and key combination that would play the tone from that generator, and played it to make sure that it did.

Manual wiring chart showing which drawbar/key combinations play each tone.
Manual wiring chart showing which drawbar/key combinations play each tone.
Tonewheel generator at 9 o'clock in the evening, after all the capacitors have been replaced.
Tonewheel generator at 9 o'clock in the evening, after all the capacitors have been replaced.

I mentioned eaerlier that the wax paper capacitors in my M-111's vibrato line box were an average of 69% higher than their indicated values. The tone generator filter capacitors were significantly worse. Of all the 0.105µF capacitors, the best one measured 0.22µF, or just over twice its original value. The worst one was at 0.40µF, or almost four times its original value, resulting in a filter that was out of tune by nearly an octave!

Recalibration

Although I had been measuring and recording the output from each tonewheel filter before and after replacing the capacitor, I wasn't doing them in numerical order, so I had no idea how close to a smooth curve they would end up being. When I finished replacing all the capacitors, the first thing I did was enter all my recorded data into a spreadsheet, sort it by tonewheel number, and graph the result:

Tonewheel generator output curve before (red) and after (blue) capacitor replacement.
Tonewheel generator output curve before (red) and after (blue) capacitor replacement. Click to enlarge.

The first thing that is immediately apparent is that the outputs were uniformly higher after replacing the capacitors (the first six outputs, #44 to #49, are from filters that do not use capacitors and thus did not change). The second thing that jumps out is that the calibration isn't even close to smooth.

Choosing a Calibration Curve

The official factory calibration curves have been lost in the mists of time, although there is at least one vendor that claims to know what they are. To fill this information void, Hammond enthusiast Kon Zissis has collected calibration curves from dozens of organs, including later model ones with mylar capacitors (which do not change in value over time). From this data, one can arrive at a good guess as to what the original curves looked like.

The curves likely varied from one series of organ to another. For instance, in the M-100 series, Hammond attempted to reduce key-click by reducing the high frequency response of the amplifier and increasing the output levels of the higher frequency tone generators to compensate for this. After perusing the various data sets in Kon's collection, I came to the conclusion that the curve for the M-100 should be straight line from tone #44 to #91, starting at 12mV and ending at 21mV peak-to-peak:

The calibration curve I decided on was a straight line (dotted grey) from 12mVpp for tone #44 to 21mVpp for tone #91.
The calibration curve I decided on was a straight line (dotted grey) from 12mVpp for tone #44 to 21mVpp for tone #91. Click to enlarge.

Preparation

There are tone generator magnets on both the front and back of the tone generator. The ones on the back can be accessed by removing the tone generator cover. To access the ones on the front, I had to remove the speaker grille panel, which is held in place with bolts from inside the organ. After undoing these and disconnecting the speakers, the panel can be pulled outward at the bottom, lowered onto the bass pedals, and then removed completely, being careful not to scratch the legs or the floor with the metal trim along the bottom of the panel. I laid the panel face down on the floor and then reconnected the speakers using alligator clip leads (it's not a good idea to operate a vacuum tube amplifier with no speakers connected).

The set-screws on the tone generator magnet collars have a 5/32" hexagonal head. Space is tight, so the best tool to use would be a 5/32" open wrench but I didn't have one handy, nor did I have a 4mm wrench (which would be only a hair bigger than a 5/32" one). I did have both 5/32" and 4mm sockets though. Despite the fact that 4mm is slightly larger than 5/32", the 4mm socket fit the screw heads more snuggly, so I used that on a screwdriver-like socket driver.

Tone generator magnet location chart from M-series service manual.
Tone generator magnet location chart from M-series service manual.
I numbered the tone generator magnets with a grease pencil.
I numbered the tone generator magnets with a grease pencil.

To make it easier to keep track of which magnet belongs to which tone, I copied the markings from the magnet location chart of the M-series service manual directly onto the tone generator using a black grease pencil.

Adjusting the Magnets

The procedure for adjusting the magnet is theoretically quite simple: loosen the set-screw, slide the magnet in or out while monitoring the filter output with an oscilloscope or peak-to-peak millivolt meter, and retighten the screw. In practice, it's not quite so easy although it's not extremely difficult either. Patience is required.

Loosen the set-screw using a 5/32" or 4mm socket wrench or open wrench.   
Loosen the set-screw using a 5/32" or 4mm socket wrench or open wrench.
The first complication is that many of the magnets may be stuck, and one has to be careful unsticking them. It is tempting to hit them with something hard like a hammer, but don't do this. Every blow will demagnetize the magnet a little, and there is the danger of the magnet being pushed hard into the spinning tonewheel. I found that the safest way to unstick the magnet was to grasp it with good pliers and try to turn it ever so slightly left and right, all the while pulling back. Of all the magnets I attempted to adjust, there was only one (#50) that I could not loosen up, but fortunately its filter output was within 1mV of where I wanted it to be.

Once the magnet is loose, one quickly discovers that it doesn't take much movement to achieve a range of output from 0mV to 50mV or more. I tried adjusting the first few magnets by carefully sliding them in or out with my fingers and then retightening the set-screw, but ran into two problems. On one magnet (#76 if I recall), I slid the magnet too far in and it contacted the tonewheel. Fortunately it was only a very light contact, and no harm appears to have been done. The other problem was that retightening the screw would invariable shift the magnet outward, resulting in a 2mV or so drop.

The technique I finally settled on is as follows:

  1. Loosen the set-screw and then unstick the magnet as necessary, as described above.

  2. If the output level is too high, retighten the set-screw until you can barely move the magnet with your fingers, and then pull the magnet out slightly until the output level is lower than what you are aiming for.

  3.    Tap gently with a plastic screwdriver handle to move the rod in a little at a time.
    Tap gently with a plastic screwdriver handle to move the rod in a little at a time.
    Retighten the set-screw just enough that you can no longer move the magnet with your fingers.
  4. Using a "soft" hard object, like a plastic screwdriver handle, gently tap the magnet inward while watching your oscilloscope or millivolt meter. If tapping gently doesn't work, loosen the set-screw a tiny bit. Don't tap any harder than you would tap yourself on the forehead with the same object.

  5. Keep tapping until the output is about 2mV higher than desired. If you go too far, loosen the screw and go back to step 2.

  6. Retighten the set screw the rest of the way. As described earlier, this usually moves the magnet out enough to drop the output by 2mV to where you want it.

  7. If it's not right, loosen the screw and go back to step 2.

I did run into an issue with one magnet, which was that in order to achieve the desired output level, I had to move the magnet so close to the tonewheel that the tone became audible directly (i.e. not through the electronics). The air gap between the magnet and wheel was so small, that the compression and decompression of the air as each tooth passed the magnet produced a physical sound. Fortunately, the sound could only be heard very faintly, and only with the tonewheel generator cover off.

Reassembly

After I adjusted the last magnet, I went back and measured the output of every tone filter again just to be sure I didn't miss one or forget to retighten the set-screw. Once I was sure everything was in order, I reinstalled the front speaker grille, the tonewheel generator cover, and the vibrato line box.

The Final Result

The chart below shows the tonewheel generator output curve that I ended up with. It's not perfectly straight, but it is always within 1mV of the straight line I was trying to achieve. At the 12mV end of the scale, 1mV represents an error of less than 1dB, and at the 21mV end, less than 0.5dB.

Tonewheel generator output curve after calibration (green). Uncalibrated (blue) and straight line (dotted grey) are shown for reference.
Tonewheel generator output curve after calibration (green). Uncalibrated (blue) and straight line (dotted grey) are shown for reference. Click to enlarge.

How Does it Sound?

The change in sound is significant, and the best way to illustrate that is with some samples. Each recording was taken directly from a line-level output installed in my M-111.

The first three recordings consist of all the keyboard tones, #18 to #91, played in succession with a gap before each C note. The tones with the white background are those that were affected by capacitor replacement. The first recording was made before replacing the capacitors, the second after replacement, and the third after recalibration.

Tones #18 to #91 before replacing the capacitors. Click image to play.
Tones #18 to #91 before replacing the capacitors. Click image to play.

Listen for the sudden drop in volume when going from the grey (non-capacitor) to the white (capacitor filtered) area. Also note that from that point forward, the amplitudes of the tones fluctuate, sometimes quite significantly.

In case you're wondering why the volume decreases at the higher frequencies even though the tonewheel generator output is increasing, it's due to the frequency response of the amplifier. Amplification drops off at the higher frequencies in a (possibly misguided) attempted by Hammond to reduce key-click.

Tones #18 to #91 after replacing the capacitors, but before recalibrating. Click image to play.
Tones #18 to #91 after replacing the capacitors, but before recalibrating. Click image to play.

After replacing the capacitors, the sudden volume drop at tone #49 was gone but the fluctuations in volume between succesive tones were still there, often even more pronounced than before. The variations in the second last octave are quite noticeable. Notice that the overall volume of the highest notes has increased significantly.

Tones #18 to #91 after replacing the capacitors and recalibrating. Click image to play.
Tones #18 to #91 after replacing the capacitors and recalibrating. Click image to play.

Once the tonewheel generator was recalibrated, the progression of tone volumes became very smooth, with two exceptions:

  • The sudden jump in volume at tone #61 was caused by switching from the 4' to the 2' drawbar to get the next octave of tones, after which the 2' tones were played to the end of the keyboard.

  • The lower volume of tone #53 was caused by a dirty key contact and this can be seen in all three recordings. I will have to shift the offending busbar to clear this up.

This next recording consists of a succession of F chords played in the root position in successive octaves of the upper manual, using the "Full Organ" preset (86 8868 446). This recording was spliced together from separate before and after recordings. Each chord is heard for about one second before capacitor replacement, followed immediately by one second with new capacitors and recalibration completed. The change is quite noticeable.

A four-octave progression of F chords before and after recapping and recalibration, played using the Full Organ preset. Click image to play.
A four-octave progression of F chords before and after recapping and recalibration, played using the Full Organ preset. Click image to play.

Conclusions

Aging wax paper capacitors have a definite detrimental effect on those tones that use them in their filters, and replacing those capacitors reverses that effect. Because the replacement capacitors will not have exactly the same values as the originals once did (due to both availability and tolerances), a recalibration will likely be necessary after capacitor replacement.

Would it make sense to leave the old capacitors and only recalibrate? Probably not, since it may not be possible to achieve the desired output levels before the magnetic rods hit the tonewheels. Even if it were, the old capacitors will continue to change over time, throwing off the calibration. Capacitor replacement is so straightforward and inexpensive, that there's no reason not to do it.

Other Articles of Interest

If you found this article useful, you may also be interested in my other Hammond organ technical articles:


 

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Last updated Wednesday October 13, 2010. E-mail Stefan

 

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